Study on the Cause of Hypoxia in the Corner of Return Air of Shallow Buried Flammable Coal Seam Group Mining Face and the Coordinated Prevention and Control of Coal Spontaneous Combustion
Abstract
:1. Introduction
Research Status of Hypoxia Problem in Working Face
2. Research Method
2.1. Background of Coal Mine
2.2. Overburden Failure Model of Shallow Coal Seam
- (1)
- Monr-Coulomb model
- (2)
- Physical model establishment
- (1)
- The total size of the established model (length × width × height) is: 2000 m × 1000 m × 329 m:
- (2)
- The step-by-step excavation process of the lower 1 coal seam and the lower 5 coal seam (as shown in Figure 3) is as follows:
- (i)
- 0 m × 80 m × 3.8 (10) m;
- (ii)
- 80 m × 160 m × 3.8 (10) m;
- (iii)
- 160 m × 240 m × 3.8 (10) m;
- (iv)
- 240 m × 320 m × 3.8 (10) m;
- (v)
- 320 m × 500 m × 3.8 (10) m;
- (vi)
- 500 m × 1100 m × 3.8 (10) m.
- (3)
- Boundary condition setting
2.3. Test of Seepage Law in Surface Fractures
- (1)
- Principle of continuous constant release of tracer gas to detect mine air leakage
- (2)
- Release device and analytical instrument
- (3)
- Measuring point arrangement
- (4)
- Air leakage detection of 5106 working face roadway
- (5)
- Check whether the goaf of 5104 and 5106 working face is connected
- (6)
- Check whether the goaf of 1112 and 5106 working face is connected
- (7)
- tracer gas sampling distance
- L—Distance between tracer gas release point and sampling point, m;
- S—Shaft section area, m2;
- U—Length of perimeter of shaft lane, m;
- (8)
- tracer gas release calculation
- —Estimated quantitative release of tracer gas, mL/min;
- K—Coefficient, value 5;
- —The air volume of roadway is 1500 m3/min at 5106 working face;
- —The minimum concentration of SF6 tracer gas in the predetermined airflow is 10−7.
3. Results and Discussion
3.1. Study on Overburden Failure Law of Mining Shallow Buried Coal Seam Group
3.2. Study on Air Leakage Law of Shallow Buried Coal Seam
- (1)
- On 7 June 2021, SF6 was released from the observation hole of the sealed wall of contact lane 5106 and 5104, with a discharge flow of 800 mL/min and a release time of 3.5 h. On the 12th of the day: After 30 min of release, SF6 gas was received at the corner of return air and 15 m away from the corner of 5106 working face. Through gas sample analysis, the maximum SF6 concentration was 0.00345 ppm, and the SF6 background concentration measured in the inlet lane was 0.00565 ppm. It can be considered that there is no air leakage between the goaf 5104 and the working face 5106.
- (2)
- SF6 was released in the 5106 transport trough on 8 June 2021, with a discharge flow of 800 mL/min and a release time of 1 h. The release begins at 13:57 and ends at 15:07. After 15 min of release, samples were taken at each measuring point successively, and analyzed by SF6 special chromatograph. It was found that the air leakage between the inlet and return air lanes was 20 m3/min.
- (3)
- On 8 June 2021, SF6 was released at the detection hole of 5106 transportation lane and 1112 goaf with a discharge flow of 25 L/min and a release time of 1.5 h. In order to accelerate the diffusion of SF6 gas in the 1112 goaf after the release, nitrogen was injected into the detection hole for 30 min. SF6 gas was measured at the corner of the return air with SF6 portable instrument and the concentration signal was the strongest. The gas was taken when the SF6 gas was detected by SF6 portable instrument and the concentration signal was the strongest. It is 380 times of the SF6 background concentration measured in the inlet roadway, which is 0.00565 ppm. It can be determined that there is air leakage between the goaf 1112 and the working face 5106. In addition, through field observation, there is an obvious gas outpouring phenomenon in the detection hole, and the pressure in the hole is 240 pa higher than that in the roadway, which also proves that the 5106 working face is connected with the 1112 goaf after mining.
- (4)
- In order to verify whether there is air leakage between the ground crack and the 5106 working face, SF6 was released at the ground crack on 15 June 2021, and the SF6 portable instrument was used for simultaneous detection at the return air corner of the 5106 working face. The release began at 11:05 on the same day with a discharge flow of 10 L/min. SF6 gas was received at the return air corner of 5106 working face at 11:29 after 24 min of release, and the concentration signal was very strong. Therefore, it could be concluded that there was air leakage between the ground crack and 5106 working face.
3.3. Formation Mechanism of Low Oxygen in Return Air Corner of Working Face
3.4. Coordinated Prevention and Control Technology System of Low Oxygen in Return Air Corner and Coal Spontaneous Combustion
- (1)
- Build a pressure zone to increase oxygen concentration in the upper cornerw
- (2)
- The upper and lower corner of the wind wall
- (3)
- Analysis of oxidation prevention and control effect of goaf residual coal
4. Conclusions
- (1)
- Based on the Monr-Coulomb model, numerical simulation tests were carried out on the failure law of overlying strata by using the command flow, and the influence of mining of the lower 1 and 5 coal seams on the overlying strata subsidence and surface penetration were obtained.
- (2)
- Based on the comprehensive consideration of atmospheric pressure, ore pressure activity, external air leakage and other factors, the mixed model of the source and emission of low oxygen gas in goaf was established, and the formation mechanism of low oxygen problem in the corner of return air of working face was defined.
- (3)
- The correlation between low oxygen in return air corner and coal spontaneous combustion was made clear. While creatively using pressure air belt to deal with low oxygen in return air corner, comprehensive fire prevention measures such as plugging, nitrogen injection and grouting were used to inhibit the oxidation of left coal in goaf and the influx of low oxygen gas to the corner, so as to achieve the goal of collaborative prevention and control of low oxygen in return air corner and coal spontaneous combustion.
- (4)
- The research results have been modified to inhibit the oxidation of residual coal and the inflow of hypoxic gas into the corner corner in the goaf, achieving the goal of the coordination prevention of hypoxic gas and spontaneous combustion of coal in the corner corner of return air. The research results have important reference significance for mine with spontaneous ignition risk or low oxygen in return air corner.
Author Contributions
Funding
Institutional Review Board Statement
Informed Consent Statement
Data Availability Statement
Conflicts of Interest
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Chen, H.; Shao, H.; Jiang, S.; Huang, C.; Liu, G.; Li, S. Study on the Cause of Hypoxia in the Corner of Return Air of Shallow Buried Flammable Coal Seam Group Mining Face and the Coordinated Prevention and Control of Coal Spontaneous Combustion. Appl. Sci. 2023, 13, 7396. https://0-doi-org.brum.beds.ac.uk/10.3390/app13137396
Chen H, Shao H, Jiang S, Huang C, Liu G, Li S. Study on the Cause of Hypoxia in the Corner of Return Air of Shallow Buried Flammable Coal Seam Group Mining Face and the Coordinated Prevention and Control of Coal Spontaneous Combustion. Applied Sciences. 2023; 13(13):7396. https://0-doi-org.brum.beds.ac.uk/10.3390/app13137396
Chicago/Turabian StyleChen, Hui, Hao Shao, Shuguang Jiang, Chenglin Huang, Guozhong Liu, and Shangguo Li. 2023. "Study on the Cause of Hypoxia in the Corner of Return Air of Shallow Buried Flammable Coal Seam Group Mining Face and the Coordinated Prevention and Control of Coal Spontaneous Combustion" Applied Sciences 13, no. 13: 7396. https://0-doi-org.brum.beds.ac.uk/10.3390/app13137396